Accident Beechcraft A35 Bonanza N595B,
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ASN Wikibase Occurrence # 42906
 
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Date:Wednesday 20 January 1993
Time:20:05 LT
Type:Silhouette image of generic BE35 model; specific model in this crash may look slightly different    
Beechcraft A35 Bonanza
Owner/operator:Rent And Lease Programs
Registration: N595B
MSN: D-1616
Total airframe hrs:4950 hours
Engine model:CONTINENTAL E-225-8
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Tulare, CA -   United States of America
Phase: Initial climb
Nature:Training
Departure airport:
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE CFI IN THE RIGHT SEAT WAS GIVING DUAL TO THE LEFT SEAT CFI, WHO HAD NO EXPERIENCE IN TYPE. DURING THE INITIAL CLIMB, AT ABOUT 400-500 FT AGL, WITNESSES HEARD THE ENGINE LOSE POWER OR SURGE. THE AIRPLANE WAS SEEN TO ROLL TO ONE SIDE AND DESCEND STEEPLY TO IMPACT. THE AIRPLANE HAD BEEN EXTENSIVELY MODIFIED WITH AN UNAPPROVED WING TIP FUEL TANK SYSTEM ADDITION. THE FUEL SELECTOR VALVE FOR THE TIP TANKS DID NOT HAVE ANY PLACARDS SHOWING POSITION OR OPERATION. BOTH CFI'S HAD BEEN GIVEN INCORRECT INSTRUCTIONS ON HOW TO POSITION THE FUEL SYSTEM SELECTOR VALVES BY THE OWNER AND A MECHANIC WHO SIGNED OFF THE ANNUAL INSPECTION. POST-CRASH EXAMINATION REVEALED THAT THE STANDARD FACTORY FUEL SELECTOR WAS IN THE AUX POSITION, AND THE TIP TANKS FUEL SELECTOR VALVE WAS IN A HALF-ON/HALF-OFF POSITION. THE AIRPLANE ALSO HAD A POWERPLANT MODIFICATION FOR INCREASED HORSEPOWER AND OTHER AIRFRAME MODIFICATIONS, NOT ALL OF WHICH WERE DOCUMENTED OR APPROVED. THIS WAS THE FIRST FLIGHT SINCE THE ANNUAL INSPECTION.

Probable Cause: THE INSTALLATION OF AN UNAPPROVED WING TIP FUEL TANK SYSTEM; AN INADEQUATE ANNUAL INSPECTION WHICH DID NOT NOTE, OR CORRECT, THE UNAPPROVED FUEL SYSTEM ADDITION; A WING TANK FUEL SELECTOR VALVE INSTALLATION WITHOUT ADEQUATE PLACARDS TO SHOW POSITION OR OPERATION; AND INCORRECT INSTRUCTIONS TO THE PILOTS BY THE OWNER AND MECHANIC ON POSITIONING FUEL SELECTOR VALVES WHICH LED TO INADVERTENT MISPOSITIONING BY THE PILOTS AND SUBSEQUENT FUEL STARVATION. IN ADDITION, THE PILOT AT THE CONTROLS FAILED TO MAINTAIN ADEQUATE AIRSPEED FOLLOWING THE POWER LOSS WHICH RESULTED IN AN INADVERTENT STALL/SPIN. A FACTOR WHICH CONTRIBUTED TO THE LOSS OF CONTROL WAS THE DARK NIGHT LIGHT CONDITION.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX93FA097
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB LAX93FA097

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
10-Apr-2024 15:55 ASN Update Bot Updated [Time, Other fatalities, Phase, Source, Narrative, Category, Accident report]

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