ASN Wikibase Occurrence # 43635
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Date: | Friday 2 November 2007 |
Time: | 14:00 |
Type: | Kelly F1D |
Owner/operator: | Private |
Registration: | N42KK |
MSN: | 001 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Reno, NV -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Test |
Departure airport: | Reno, NV (4SD) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed on his first flight in the experimental amateur-built airplane. Before departure, the pilot asked a person, who also became an eyewitness to the accident, to monitor the radio and document information regarding the test flight transmitted by the pilot. During the preflight briefing, the pilot told the witness that part of the flight would include doing an "approach to stall." The pilot topped off the 5-gallon fuel tank and departed for an estimated 30-minute flight. The witness observed the airplane maneuvering near the airport, and the pilot made several transmissions to him. The witness said the airplane entered a high downwind (approximately 2,000-3,000 feet above the ground). He observed the airplane slow to a nose high attitude while maintaining altitude. Then, while maintaining the same pitch attitude, a constant loss of altitude occurred with the wings level for approximately 3 to 4 seconds. He heard no increase in engine power nor was the airplane's pitch angle reduced. There appeared to be an abrupt entry into a right spin, and 6 to 8 turns were observed with a nearly vertical impact with the ground. Post accident examination of the engine revealed no abnormalities that would have precluded normal operation. No logbooks documenting airplane maintenance were found, and no pilot flight logbooks were found.
Probable Cause: The pilot's loss of airplane control while performing intentional approach to stall maneuvers. Contributing to the accident was the inadvertent entry of the airplane into a spin.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA08LA017 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20071109X01779&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Dec-2017 19:00 |
ASN Update Bot |
Updated [Cn, Operator, Other fatalities, Nature, Destination airport, Source, Narrative] |
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