ASN Wikibase Occurrence # 43784
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Date: | Friday 18 May 2007 |
Time: | 08:15 |
Type: | Cessna 150G |
Owner/operator: | Private |
Registration: | N3121J |
MSN: | 15065821 |
Year of manufacture: | 1966 |
Total airframe hrs: | 2393 hours |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Pahrump, Nevada (at approx co-ordinates 36'25" N, 115'99" W) -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Pahrump, NV (NV00) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Witnesses reported the airplane departed on runway 18, and approximately 50 feet above the ground, the engine began to sputter. It started to turn left, back towards the airfield, and descend in a left wing low, nose-low attitude to ground impact. The airplane's empennage failed in a scorpion like manner and it came to rest inverted. The most recent 100-hour/annual inspection was performed on April 23, 2007, with a tachometer time of 2,393 hours. The airplane had been flown approximately 7 hours during the last 13 months. No preimpact mechanical engine or airframe anomalies, which might have affected the airplane’s performance, were identified. A decal near the left fuel tank filler port indicated the use of auto-gas was approved, but no associated FAA Major Repair and Alteration form 337 was found in the aircraft paperwork. The right fuel tank was breached and did not contain fuel. The left fuel tank contained yellow colored fuel. The firewall mounted fuel strainer screen was discolored, and the reservoir contained brownish-yellow fuel, which was contaminated with dirt and tested positive for water. The carburetor inlet screen was partially obstructed with dirt, rust, and sand.
Probable Cause: The loss of engine power due to fuel contamination followed by the pilot's failure to maintain aircraft control during takeoff. Contributing factors were the pilot's inadequate preflight and an inadequate 100-hour maintenance inspection by other maintenance personnel.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA07LA126 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070608X00698&key=1 FAA register: 2.
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=3121J Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
04-Mar-2015 23:24 |
Dr. John Smith |
Updated [Operator, Location, Departure airport, Source, Narrative] |
04-Mar-2015 23:25 |
Dr. John Smith |
Updated [Location, Destination airport] |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Dec-2017 18:37 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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