Accident Van's RV-7A N216RV,
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ASN Wikibase Occurrence # 43929
 
This record has been locked for editing.

Date:Saturday 2 December 2006
Time:08:45
Type:Silhouette image of generic RV7 model; specific model in this crash may look slightly different    
Van's RV-7A
Owner/operator:Private
Registration: N216RV
MSN: 70256
Engine model:Aero Engines IO-360
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Norman, OK -   United States of America
Phase: Approach
Nature:Private
Departure airport:Midwest City, OK (2OK2)
Destination airport:Norman, OK (OUN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The 325-hour private pilot lost control of the single-engine homebuilt airplane while initiating the approach and landing phase of the flight. The accident airplane was selected to be the last to land in trail as a flight of three. The tower operator cleared the flight of 3 airplanes to land on Runway 03. The tower operator reported that as he watched the first airplane land, he noticed the sun reflect off the third airplane and observed it go below a tree line. Numerous witnesses observed the accident airplane approach the airfield. Several witnesses reported that the airplane was low or very low, and as it approached the airfield. The witnesses observed the accident airplane made a sharp bank, just before impacting the ground. Furthermore, one of the witnesses stated that the airplane was "struggling, tipping left-and-right, and he thought it was going to tip over" before entering a sudden 90-degree turn and assuming a pronounced nose-low attitude. The pilots of the other two airplanes in the flight, stated that prior to the flight they had agreed to slow their airplanes to 70 mph, and then to 65 mph in order to maintain proper spacing between the airplanes during their approach to land. Flight control continuity was established and the flaps were confirmed to be in the fully extended position. An examination of the airplane and engine did not reveal any anomalies that prevented normal operation.
Probable Cause: The pilot's failure to maintain airspeed which resulted in an inadvertent stall. A contributing factor was the pilot's attempt at formation flying.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DFW07LA032
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20061207X01753&key=1

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Aug-2016 20:04 junior sjc Updated [Operator]
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
20-Aug-2017 06:59 junior sjc Updated [Nature, Departure airport, Destination airport, Narrative]
05-Dec-2017 09:31 ASN Update Bot Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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