ASN Wikibase Occurrence # 43958
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Date: | 05-NOV-2006 |
Time: | 01:24 |
Type: | Cessna 172S |
Owner/operator: | Yingling Aircraft, Inc. |
Registration: | N53443 |
MSN: | 172S9370 |
Fatalities: | Fatalities: 2 / Occupants: 4 |
Other fatalities: | 0 |
Aircraft damage: | Written off (damaged beyond repair) |
Category: | Accident |
Location: | near Hominy, Osage County, OK -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Tulsa Municipal Airport, OK (TUL/KTUL) |
Destination airport: | Wichita Dwight D. Eisenhower National Airport, KS (ICT/KICT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Dark night instrument conditions prevailed throughout the area when the non-instrument rated private pilot elected to initiate the 114-nautical mile cross-country flight to his home station. There were no witnesses to the accident. The moon illumination on the night of the accident was reported as full moon; however, there was an overcast sky, and visibility was reduced due to rain and the cloud layer. Additionally, the unpopulated terrain over the route of flight provided little illumination for ground references. Search and rescue operations were hampered due to IFR conditions in the area, and the wreckage was not located for 4 hours and 29 minutes following the accident. The investigation revealed that the pilot had accumulated a total of 4.1 hours of night time, and 4.0 hours of simulated instrument time. The single-engine airplane impacted the ground on a heading of 240-degrees, coming to rest in inverted, 501-feet from the initial impact point. Ground scars, and damage sustained by the airframe, were consistent with the airplane impacting the ground in the cruise configuration in a near level flight attitude. The flaps were found in the fully retracted position. No anomalies were found with the airframe or the engine that could have prevented normal flight operations. Flight and engine control continuity was established at the accident site.
Probable Cause: The pilot's continued cruise flight into adverse weather conditions, and his failure to maintain clearance from terrain. Contributing factors were the dark night conditions, and the low ceilings.
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20061109X01633&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
05-Dec-2017 09:29 |
ASN Update Bot |
Updated [Operator, Source, Narrative] |
05-Jan-2023 05:40 |
Ron Averes |
Updated [Location, Departure airport, Destination airport] |
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