Accident de Havilland Canada DHC-2 Beaver N5154G,
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ASN Wikibase Occurrence # 44006
 
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Date:Thursday 21 September 2006
Time:13:15
Type:Silhouette image of generic DHC2 model; specific model in this crash may look slightly different    
de Havilland Canada DHC-2 Beaver
Owner/operator:Alaska Sportsman's Lodge, LLC.
Registration: N5154G
MSN: 405
Total airframe hrs:11613 hours
Engine model:Pratt & Whitney R-985-14-B
Fatalities:Fatalities: 1 / Occupants: 6
Aircraft damage: Substantial
Category:Accident
Location:75 mi NW of Kodiak, AK -   United States of America
Phase: Take off
Nature:Unknown
Departure airport:Kodiak, AK
Destination airport:Igiugig, AK
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airline transport pilot was departing to the north from a narrow stream in a float-equipped airplane with lodge guests aboard, on a Title 14, CFR Part 91 flight. Northerly winds between 25 and 35 knots, were reported at the time of the accident. The accident pilot reported that after departure, he turned left, and a strong downdraft "threw the airplane to the ground." The passengers said that the airplane started its takeoff run directly into the strong winds, but shortly after becoming airborne, the pilot made a steep turn to the left, about 150 feet above the ground. The passengers indicated that as the airplane continued to turn left, it began to shudder and buffet, then abruptly descended nose low into the marsh-covered terrain. During the impact, the right wing folded, and the airplane's fuselage came to rest on its right side. One of the occupants, seated next to the right main cabin door, was partially ejected during the impact sequence, and was pinned under the fuselage and covered by water. Rescue efforts by the pilot and passengers were unsuccessful. In the pilot's written statement to the NTSB, he reported that there were no preaccident mechanical anomalies with the airplane, and during the on-site examination of the wreckage by the NTSB investigator-in-charge, no preaccident mechanical anomalies were discovered.




Probable Cause: The pilot's failure to maintain adequate airspeed while maneuvering to reverse direction, which resulted in an inadvertent stall and an uncontrolled descent. Factors associated with the accident were the inadvertent stall and wind gusts.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC06FA136
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20060928X01423&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
14-Aug-2011 11:09 TB Updated [Time, Operator, Total occupants, Location, Nature, Departure airport, Destination airport, Source, Damage, Narrative]
14-Aug-2011 11:15 TB Updated [Cn, Operator, Departure airport]
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
05-Dec-2017 09:25 ASN Update Bot Updated [Cn, Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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