ASN Wikibase Occurrence # 44598
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Date: | Saturday 8 January 2005 |
Time: | 08:15 |
Type: | Cessna 150J |
Owner/operator: | Private |
Registration: | N51256 |
MSN: | 15069875 |
Year of manufacture: | 1968 |
Total airframe hrs: | 5084 hours |
Engine model: | Continental O-200A |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Marana, AZ -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Marana, AZ (AVQ) |
Destination airport: | Marana, AZ (AVQ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane collided with power lines while maneuvering at low altitude. The airplane owner said the pilot had stopped by his residence around 0600 on the morning of the accident to ask if he could take the owner's daughter on the flight. The owner indicated that it was too early to get her up, so the pilot went to the airport by himself. Around the time of the accident the owner and his spouse were in their front yard with their coffee and newspaper walking towards the back of the house when they saw the accident airplane. The airplane made one low pass over them. On the second pass, the airplane was headed to the west, and crossed over the north-to-south power lines. They continued toward the back of their house as the airplane made the turn back toward the house. The owner then heard the sounds of the airplane contacting the power lines. As he came to the front of the house, the owner saw the airplane coming to its final resting place about 150 feet from the power lines with its nose in the ground. The poles that held the lines were measured at a height of 47 feet above ground level. The static power lines were about 2 feet below that, at a height of 45 feet. The most westerly static power line had been cut. The other cable wrapped around the airplane; however, it remained connected to the poles. The airframe and engine were inspected. Investigators established flight control continuity and engine continuity. There were no mechanical anomalies found that would have precluded normal operation of the airplane.
Probable Cause: the failure of the pilot to maintain an adequate altitude and clearance from obstructions that resulted in an in-flight collision with power lines.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX05FA062 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20050120X00087&key=1
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
06-Dec-2017 06:52 |
ASN Update Bot |
Updated [Operator, Other fatalities, Source, Narrative] |
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