Accident Cessna 337B Super Skymaster N133JW,
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ASN Wikibase Occurrence # 44643
 
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Date:Tuesday 16 November 2004
Time:16:11
Type:Silhouette image of generic C337 model; specific model in this crash may look slightly different    
Cessna 337B Super Skymaster
Owner/operator:Private
Registration: N133JW
MSN: 337-0612
Total airframe hrs:4108 hours
Fatalities:Fatalities: 3 / Occupants: 3
Aircraft damage: Destroyed
Category:Accident
Location:Drake, AZ -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Survey
Departure airport:Williams, AZ (KP32)
Destination airport:Williams, AZ (KP32)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The twin-engine airplane impacted terrain while performing a low altitude maneuvering turn. The pilot had been taking hunters on elk scouting flights for a number of days prior to the accident. These flights were conducted below 500 feet above ground level (agl) in the same general area that the accident occurred. A videotape of the airplane on a previous scouting trip shows it flying slightly above the horizon with the landing gear extended over the local desert terrain and ridges. The first identifiable point of impact contained green glass fragments from the right wing position light. The right main landing gear strut was separate from the main wreckage, in the debris field, indicating it was probably deployed, and the flap jackscrew corresponded to a 10-degree flap position. This flight configuration is consistent with the observed configuration of the airplane during previous scouting flights. A handheld global positioning system (GPS) receiver recovered at the accident site recorded the airplane's flight path leading up to the accident. The ground track and speeds recorded by the GPS has the airplane entering a left-hand turn at 70 kts. Halfway through the turn the speed bled down to 59 kts. According to the airplane's Pilot Operating Handbook, a level 30-degree angle of bank turn with the landing gear deployed and the flaps at 8 degrees, the airplane will stall at 66 kts. While in a left-hand turn the airplane experienced an accelerated stall, entered an uncontrolled descent in which the pilot did not have enough altitude to recover from, and impacted terrain in a right wing down attitude. Examination of the wreckage revealed no evidence of a preimpact malfunction or failure of the control system, or power plants.
Probable Cause: the pilot's failure to maintain airspeed above stall speed while maneuvering at low altitude, which resulted in an accelerated stall and spin. A factor in the accident was the pilot's performance of maneuvering flight at an altitude insufficient to allow for recovery from an accelerated stall.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX05FA035
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20041129X01872&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Dec-2017 18:32 ASN Update Bot Updated [Operator, Source, Narrative]

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