Accident Lancair 360 N163DS,
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ASN Wikibase Occurrence # 44710
 
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Date:Friday 10 September 2004
Time:14:40
Type:Silhouette image of generic LNC2 model; specific model in this crash may look slightly different    
Lancair 360
Owner/operator:Private
Registration: N163DS
MSN: 751
Engine model:Lycoming IO-360-B
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Orange, TX -   United States of America
Phase: Take off
Nature:Private
Departure airport:Orange, TX (KORG)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
A 642-hour pilot departed from an airfield and announced that he would be circling around the traffic pattern to make a low pass. A witness stated that he observed the airplane as it approached the runway with the landing gear extended. The witness described the airplane's speed as "moderate" as it passed over the runway at a height of 50 feet above the ground. As the airplane reached the end of the runway it began to climb at a pitch attitude of approximately 10-15 degrees. As the witness began to enter a building, he looked back toward the departure end of the runway and saw the airplane in a rapid descent. It was approximately 600 feet above the ground, the nose of the airplane was pitched down about 30 degrees, and it was in a 10-15 degree right bank. When the airplane was approximately 100-150 feet above the ground, the witness stated the airplane pitched up (about five degrees) and the wings leveled out, but it still continued to descend. The witness did not hear any engine noise during this time. The nose of the airplane continued to pitch up and it banked slightly to the left as it descended behind a tree line. He then heard the engine "roar to what sounded like full power," followed by the sound of an impact. The pilot's total flight time in the make and model could not be determined; however, it was determined that the pilot had recently purchased the airplane as the registration was still pending.
Probable Cause: The pilot's failure to maintain adequate airspeed during takeoff resulting in an inadvertent stall and loss of aircraft control.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW04LA236
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20040916X01440&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Dec-2017 18:22 ASN Update Bot Updated [Operator, Source, Narrative]

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