ASN Wikibase Occurrence # 45804
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Date: | Saturday 21 July 2001 |
Time: | 12:45 |
Type: | Smith Kelly-D |
Owner/operator: | Private |
Registration: | N303SM |
MSN: | 38 |
Total airframe hrs: | 60 hours |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Poplar Grove , IL -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Poplar Grove, IL (C77) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The amateur-built experimental biplane was destroyed when it experienced an in-flight separation of the right upper wing and spiraled into the terrain. A witness reported that he saw, "the Kelly-D airplane coming out of a maneuver of some kind. He continued west at approx. 800-1000'. He pulled up, rolled to the left (inverted) and pulled out (1/2 loop). He repeated the same maneuver going east, and as he leveled out I saw what looked like a large piece of fabric and another object leave the airplane. The fabric fell slowly the other object a little faster. The airplane continued for a couple seconds and then rolled over and spiraled into the ground." The witness reported the maneuver was smooth and that it could not have pulled more that 3.5g's during the maneuver. He reported the failure occurred as the airplane was leveling off. He reported the engine was operating during the entire flight and there was no indication of an engine problem. One of the wooden propeller blades was found bent opposite the direction of rotation, broken at the hub, and was splintered. A propeller slash was found in the dirt at the point of propeller impact. The clevis ends of the flying and landing wires were examined. Six of the jam nuts were found loose. The examination of the left front upper spar revealed that the adhesive used on the plywood doubler did not cover the entire area being bonded to the spar. The USDA Forest Products Laboratory report stated, "There was also very little penetration of the adhesive into the spar." The report stated that the right upper front and rear spars exhibited compression and tension failure surfaces.
Probable Cause: The right upper wing failed due to overload. A factor was the pilot performing aerobatic manuevers.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI01FA232 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20010727X01532&key=1 Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Dec-2017 11:49 |
ASN Update Bot |
Updated [Departure airport, Source, Narrative] |
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