Accident Taylorcraft BC-12D N39971,
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ASN Wikibase Occurrence # 45900
 
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Date:Saturday 6 November 2004
Time:16:34
Type:Silhouette image of generic TAYB model; specific model in this crash may look slightly different    
Taylorcraft BC-12D
Owner/operator:Private
Registration: N39971
MSN: 6630
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Wasta, SD -   United States of America
Phase: Approach
Nature:Private
Departure airport:Wasta, SD (PVT)
Destination airport:Wasta, SD (PVT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane impacted terrain after suffereing a loss of engine power followed by a loss of control. The student pilot was returning to land at his farm field when the accident occurred. A witness reported seeing the airplane's wing "wobble" when it was at an altitude of about 300 feet above the ground prior to it descending to impact. He stated he was in a vehicle at the time and was unable to tell if the engine was operating. The accident occurred at sunset and the airplane was not equipped with any cockpit lighting. Post accident examination of the airplane revealed it impacted the terrain in a nose down, left wing low attitude. One of the wooded propeller blades was shattered and the other was intact. The mixture control was in and the pushpull type fuel shutoff valve was pulled to the off position. The fuel shutoff valve was bent upward and formed around the instrument panel. The carburetor heat control was pushed in. Airworthiness Directive (AD) 51-09-03 applied to the accident airplane. The AD stated that a safety device must be installed on the fuel shutoff valve to prevent inadvertent operation of the valve while in flight. The safety device was installed; however, it was bent so that it was not covering the fuel shutoff valve. No discrepancies were noted during the engine teardown that would have prevented the engine from producing power.



Probable Cause: The pilot inadvertently pulled the fuel shut off valve resulting in fuel starvation and a subsequent loss of engine power. The pilot also failed to maintain adequate airspeed which resulted in the airplane stalling.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI05LA023
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20041109X01792&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Dec-2017 18:32 ASN Update Bot Updated [Source, Narrative]

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