ASN Wikibase Occurrence # 48614
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 7 December 2008 |
Time: | 16:19 |
Type: | Rocket F-1 Evo |
Owner/operator: | Stephen Merrell |
Registration: | N757SM |
MSN: | 150 |
Total airframe hrs: | 135 hours |
Engine model: | MATTITUCK TMX-540 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sebastian, FL -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Sebastian, FL (X26) |
Destination airport: | Sebastian, FL (X26) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot of the amateur-built airplane elected to operate the airplane on the accident date with the fuel selector positioned to the right tank, and flew to a nearby airport where he performed an uneventful full-stop taxi-back landing. The pilot initiated takeoff with the fuel selector positioned to the right tank which was nearly empty and contrary to the Before Take Off checklist, and remained in the traffic pattern. While on the downwind leg abeam the approach end of the intended runway with another airplane on the extended downwind leg, the engine experienced a loss of power due to fuel starvation. He regained control of the airplane, which took 15 to 20 seconds, maintained best glide airspeed and then turned towards the runway. Unable to land on the runway, he maneuvered the airplane for a forced landing, but before ground contact he switched the fuel selector to the left tank position. Engine power was not restored and the airplane was substantially damaged during the off-airport forced landing. Postaccident examination revealed, a total of approximately 15 gallons of fuel in the left fuel tank, while the right fuel tank was empty. The fuel tanks were not breached and there was no evidence of fuel leakage at the scene.
Probable Cause: A loss of engine power due to fuel starvation as a result of the pilot's incorrect positioning of the fuel selector valve.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09LA081 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
08-Dec-2008 11:08 |
harro |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 12:13 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation