ASN Wikibase Occurrence # 59575
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Date: | Friday 17 April 2009 |
Time: | 11:15 |
Type: | Cessna 421B |
Owner/operator: | Private |
Registration: | N1935G |
MSN: | 421B0836 |
Year of manufacture: | 1974 |
Engine model: | Continental GTSIO-520-H |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Andrews Ave, Oakland Park, Florida -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Fort Lauderdale, FL (FXE) |
Destination airport: | Fernandina, FL (55J) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Prior to the accident flight witnesses observed the pilot "haphazardly" pouring oil into the right engine. The pilot then ran the engines at mid-range power for approximately 20 minutes. The airplane subsequently taxied out of the ramp area and departed. Fire was observed emanating from the right engine after rotation. The airplane continued in a shallow climb from the runway, flying low, with the right engine on fire. The airplane then banked right to return to the airport and descended into a residential area. Examination of the right engine revealed an exhaust leak at the No. 4 cylinder exhaust riser flange. Additionally, one of the flange boltholes was elongated, most likely from the resulting vibration. The fuel nozzle and B-nut were secure in the No. 4 cylinder; however, its respective fuel line was separated about 8 inches from the nozzle. No determination could be made as to when the fuel line separated (preimpact or postimpact) due to the impact and postcrash fire damage. Examination of the right engine turbocharger revealed that the compressor wheel exhibited uniform deposits of an aluminum alloy mixture, consistent with ingestion during operation, and most likely from the melting of the aluminum fresh air duct. Additionally, the right propeller was found near the low pitch position, which was contrary to the owner's manual emergency procedure to secure the engine and feather the propeller in the event of an engine fire.
Probable Cause: The pilot's failure to maintain aircraft control and secure the right engine during an emergency return to the airport after takeoff. Contributing to the accident was an in-flight fire of the right engine for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09FA248 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB
https://wtop.com/?nid=104&sid=1652327_ https://flightaware.com/live/flight/N1935G ]Sun Sentinel https://www.ntsb.gov/ntsb/brief.asp?ev_id=20090417X30037&key=1 Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
17-Apr-2009 10:06 |
slowkid |
Added |
17-Apr-2009 11:58 |
harro |
Updated |
18-Apr-2009 11:29 |
harro |
Updated |
24-Apr-2009 01:29 |
slowkid |
Updated |
24-Mar-2010 13:10 |
harro |
Updated [Source] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 18:54 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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