ASN Wikibase Occurrence # 66071
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Date: | Wednesday 1 July 2009 |
Time: | 09:30 |
Type: | Republic RC-3 Seabee |
Owner/operator: | Private |
Registration: | N87487 |
MSN: | 38 |
Total airframe hrs: | 1192 hours |
Engine model: | Franklin 6A8 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Burley, Idaho -
United States of America
|
Phase: | Initial climb |
Nature: | Training |
Departure airport: | Burley, ID |
Destination airport: | Caldwell, ID (EUL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The student pilot reported that despite his request for the airplane to be refueled with 30 gallons of fuel prior to takeoff, the fixed base operator had filled the airplane with 67.7 gallons of fuel. The flight instructor reported that after the student pilot was notified that the airplane had been topped off with fuel, he "ran the numbers in [his] head and determined it would be fine because of the same conditions that were present" for takeoff from a different airport earlier in the day. The student pilot reported that while on the initial climb from the airport, the airplane stopped climbing and began to descend. At an altitude of 100 feet above ground level, the flight instructor took control of the airplane to ensure a proper climbout speed was maintained. The airplane continued to descend and collided with power lines. Subsequently, the airplane nosed over and impacted the ground in a vacant lot. A witness reported that the airplane slowly accelerated down the 4,067-foot-long runway and used approximately 85 to 90 percent of the available runway to become airborne. The witness observed the airplane "climbing at an extremely slow rate," and stated it appeared that "the pilot attempted to increase the rate of climb twice," which resulted in the airplane’s "left wing starting to dip as it appeared to be approaching a stall." Examination of the airplane by a Federal Aviation Administration inspector revealed that the empennage had separated from the fuselage just aft of the cabin and that the rudder, vertical stabilizer, nose, and wings were structurally damaged. No mechanical anomalies were noted with the engine or airframe. Takeoff performance calculations for the reported weather conditions revealed that the airplane’s required takeoff distance to clear a 50-foot obstacle was 3,921 feet on a paved surface.
Probable Cause: The flight instructor's failure to maintain clearance from power lines during takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR09LA323 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
01-Jul-2009 20:57 |
slowkid |
Added |
01-Jul-2009 21:50 |
slowkid |
Updated |
02-Jul-2009 02:58 |
slowkid |
Updated |
25-Nov-2009 03:08 |
slowkid |
Updated |
25-Nov-2009 03:11 |
Anon. |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 15:49 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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