ASN Wikibase Occurrence # 66329
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Date: | Tuesday 7 July 2009 |
Time: | 13:00 |
Type: | Air Tractor AT-301 |
Owner/operator: | AG-FLIGHT INC |
Registration: | N8587S |
MSN: | 301-0153 |
Year of manufacture: | 1978 |
Total airframe hrs: | 9004 hours |
Engine model: | P&W R1340 SERIES |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Decatur County, Georgia -
United States of America
|
Phase: | En route |
Nature: | Training |
Departure airport: | Bainbridge, GA (BGE) |
Destination airport: | Bainbridge, GA (BGE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was progressing with his aerial application training. He was supposed to depart the airport, perform steep turns and flight at minimum controllable airspeed, drop water at a designated spot about 3/4 mile from the airport, and return for landing. The airplane was observed about 5 miles west of the airport, in level flight from north to south. The airplane then made a left U-turn and flew from south to north. The airplane made another left turn, toward the west, and started climbing. The airplane then released water and instantly began a fast spiral straight down to the ground, with the water following. Witnesses heard loud, continuous engine noise throughout the accident sequence and several examinations of the wreckage did not reveal evidence of any preimpact mechanical malfunctions. The pilot received his private pilot certificate about 5 weeks prior to the accident and had conducted his previous training in an airplane with less than one-third the horsepower and one-half the weight-carrying capacity as the accident airplane. The pilot had accumulated 2 hours of flight experience in the accident airplane when the accident occurred. Additionally, both airplanes displayed a tendency to pitch up during a water drop maneuver, though the accident airplane displayed this characteristic more severely due to its higher weight. This tendency would require a pilot to aggressively push the flight control stick forward, near the stop, to counteract the force.
Probable Cause: The pilot's failure to maintain adequate airspeed while maneuvering, which resulted in an aerodynamic stall. Contributing to the accident was the pilot's lack of experience in the make and model airplane.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09LA385 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
08-Jul-2009 10:25 |
slowkid |
Added |
08-Jul-2009 11:58 |
harro |
Updated |
08-Jul-2009 16:39 |
RobertMB |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 15:48 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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