ASN Wikibase Occurrence # 70010
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 8 November 2009 |
Time: | 11:30 |
Type: | Beechcraft A36 Bonanza |
Owner/operator: | Private |
Registration: | N91TD |
MSN: | E-2624 |
Year of manufacture: | 1991 |
Total airframe hrs: | 2744 hours |
Engine model: | Continental IO-550-B(6) |
Fatalities: | Fatalities: 3 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bulverde, near Ahern Creek Drive northwest of Kestrel Airpark, TX -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Kerrville, TX (KERV) |
Destination airport: | Pearland, TX (KLVJ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was on an instrument flight rules flight and was level at 9,000 feet mean sea level. Radar data showed that the airplane was flown in an area of heavy intensity rain echoes and was on a meandering course generally eastbound when it then began a shallow turn to the left and then began turning to the right. Radar data for the last 14 seconds of the flight showed that the airplane began a descent and was still turning to the right. Radio and radar contact was then lost. Two witnesses near the accident site reported hearing a loud noise and then seeing something very large with lots of smaller pieces falling out of the clouds. Separated portions of the airplane impacted terrain in a generally circular area about 500 feet in diameter, consistent with an in-flight breakup at a low altitude.
A postaccident examination of the airplane showed no anomalies with the engine or other systems. A review of the pilot’s logbook showed that his last instrument flight experience was nearly 2 years prior to the accident. It also showed the pilot had recently purchased the airplane and had approximately 4 hours of flight time in it. A sedating antihistamine with impairing effects was found during a postmortem toxicological examination of tissue from the pilot, but no blood was available for analysis, so no determination could be made regarding how recently the medication might have been taken or whether the pilot could have been impaired by its use at the time of the accident.
Probable Cause: The pilot's failure to maintain control of the airplane during cruise flight in instrument meteorological conditions. Contributing to this accident was the pilot’s lack of recent experience in flying in instrument meteorological conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN10FA044 |
Status: | Investigation completed |
Duration: | 2 years 1 month |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
08-Nov-2009 16:11 |
RobertMB |
Added |
08-Nov-2009 16:12 |
RobertMB |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 17:49 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation