ASN Wikibase Occurrence # 73749
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Date: | Thursday 1 April 2010 |
Time: | 12:53 |
Type: | Beechcraft B36TC Bonanza |
Owner/operator: | Poelking Air Llc |
Registration: | N4BA |
MSN: | EA-356 |
Year of manufacture: | 1983 |
Total airframe hrs: | 2284 hours |
Engine model: | Continental TSIO-520 SER |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | near Dayton-Wright Brothers Airport, OH -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Dayton-Wright Brothers Airport, OH (MGY/KMGY) |
Destination airport: | Chicago-Dupage County Airport, IL (DPA/KDPA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Approximately 1 minute after takeoff, as the airplane was about 1 mile southwest of the airport, the pilot reported an engine failure to air traffic controllers and initiated a return to the airport. One witness, located about 1 mile west of the airport, reported that the sound of the engine changed abruptly; noting that the engine seemed to lose power completely. Another witness, located near the airport, observed the airplane approach from the west and turn to align with the downwind runway. During the turn, the left wingtip struck the ground and the airplane impacted short of the runway, near Penny Royal Road. A post impact fire ensued. Although the pilot initiated a return to the airport, an interstate highway and an open grass area short of the runway were both potentially available for an emergency landing. A postaccident examination of the engine revealed that the No. 1 (aft) main crankshaft bearing failed due to unknown circumstances. The progressive failure of the bearing likely precipitated secondary failures of the crankcase through-bolt and the fuel pump coupling, which resulted in a complete loss of engine power.
Probable Cause: The complete loss of engine power due to failure of the No. 1 main bearing, and the secondary failure of a crankcase through-bolt and the fuel pump drive coupling. Contributing to the accident was the pilot's decision to attempt a return to the airport for a downwind forced landing, despite having an interstate highway and an open grass area short of the runway as available emergency landing sites.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN10FA180 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB
https://www.journal-news.com/news/hamilton-news/plane-crash-kills-2-at-wright-brothers-airport-631568.html_ https://www.whio.com/news/23025859/detail.html http://www.thaindian.com/newsportal/world/two-killed-after-small-plane-crashes-near-dayton-oh-airport_100342370.html https://flightaware.com/live/flight/N4BA http://www.airport-data.com/aircraft/photo/000368938L.html (photo)
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
01-Apr-2010 13:54 |
RobertMB |
Added |
01-Apr-2010 14:10 |
RobertMB |
Updated [Aircraft type, Registration, Cn, Operator, Destination airport, Source] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 16:36 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
21-Sep-2023 04:40 |
Ron Averes |
Updated [[Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]] |
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