ASN Wikibase Occurrence # 73966
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Date: | Friday 16 April 2010 |
Time: | 19:06 |
Type: | Cessna 182 Skylane |
Owner/operator: | Aerial Advertising |
Registration: | N5318B |
MSN: | 33318 |
Year of manufacture: | 1956 |
Engine model: | Teledyne Continental O-470U |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near North Johnson Avenue and Fesler Street, El Cajon, CA -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | El Cajon, CA (SEE) |
Destination airport: | El Cajon, CA (SEE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he flew around the local area and was going to orbit his parent’s house before heading inbound for landing. He stated that he applied carburetor heat for the descent to 2,000 feet for his orbit. During the second orbit, he heard and felt the engine sputter, and then go to idle. He immediately leveled the wings, turned the airplane toward the airport, exercised the throttle, and reported to an air traffic controller that he was inbound for landing. When he did not get the expected engine rpm, he again applied carburetor heat. He slowed the airplane to the best glide speed, and again exercised the throttle. A rise in manifold pressure was noted, but not rpm, when he increased the throttle. After determining that he could not make the airport, he decided to land on a city street. He tried to avoid power lines and telephone cables in his flight path, but was unsuccessful. The airplane subsequently impacted the ground at a 35-degree nose down angle, skidded to a stop, and caught fire shortly thereafter. During a postaccident inspection of the engine, no anomalies were noted that would have precluded normal operation. The pilot stated that he completed a thorough preflight. The airplane had more than 1/2 tank of fuel in the left wing, and just over 1/4 tank of fuel in the right wing. The fuel gauges agreed with the visual inspection. A graph in the Federal Aviation Administration Special Airworthiness Information Bulletin (SAIB) CE-09-35 illustrated that the conditions encountered in this accident were at the boundary of the areas for serious icing for both glide and cruise power. Given the lack of any mechanical anomalies it is likely that the formation of carburetor ice resulted in the loss of engine power.
Probable Cause: The pilot's delayed use of carburetor heat while operating in conditions conducive to carburetor icing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10LA209 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
17-Apr-2010 02:21 |
RobertMB |
Added |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 16:34 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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