ASN Wikibase Occurrence # 75952
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Date: | Tuesday 27 July 2010 |
Time: | 11:00 |
Type: | Beechcraft B55 Baron |
Owner/operator: | Edward C Judd |
Registration: | N33CJ |
MSN: | TC-1074 |
Total airframe hrs: | 2196 hours |
Engine model: | Teledyne-Continental IO-520-E |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Oceanside Municipal Airport (KOKB), Oceanside, California -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Orchid Beach-Fraser Island Airport, QLD (OKB) |
Destination airport: | Orchid Beach-Fraser Island Airport, QLD (OKB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:One witness reported that, during the airplane's initial climb, the engines seemed out of synchronization, and the airplane was yawing and drifting to the right and wasn’t gaining altitude before it rolled to the right in a descent and went out of view. A second witness reported that one engine didn’t sound like it was producing full power, like it was sputtering, and another witness observed the low-flying airplane’s landing gear retract before it rolled to the right and crashed. The airplane impacted terrain in an open field in a slightly right-wing-low attitude, came to rest upright, and sustained extensive thermal damage to the cabin and cockpit, obliterating any evidence of switch or control lever position or instrument indication. A postaccident examination of the airframe, engines, and propellers revealed no evidence of mechanical failure or malfunction that would have precluded normal operation. Examination of the propellers revealed signatures consistent with the left engine producing low power and the right engine producing no power at ground impact.
Probable Cause: The pilot’s failure to maintain directional control of the airplane following a loss of power in the right engine. The reason for the loss of power in the right engine could not be determined.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10FA369 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
27-Jul-2010 13:20 |
slowkid |
Added |
27-Jul-2010 13:20 |
slowkid |
Updated [Other fatalities, Phase, Departure airport, Damage] |
27-Jul-2010 16:36 |
RobertMB |
Updated [Aircraft type, Operator, Source] |
27-Jul-2010 16:39 |
RobertMB |
Updated [Aircraft type, Narrative] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 17:58 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
05-Jun-2023 10:11 |
Ron Averes |
Updated [[Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]] |
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