Loss of pressurization Accident Boeing 757-223 (WL) N626AA,
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Date:Tuesday 26 October 2010
Time:21:30
Type:Silhouette image of generic B752 model; specific model in this crash may look slightly different    
Boeing 757-223 (WL)
Owner/operator:American Airlines
Registration: N626AA
MSN: 24584/304
Year of manufacture:1990
Total airframe hrs:63010 hours
Engine model:Rolls Royce RB.211 SERIES
Fatalities:Fatalities: 0 / Occupants: 160
Aircraft damage: Substantial
Category:Accident
Location:near Miami, FL -   United States of America
Phase: En route
Nature:Passenger - Scheduled
Departure airport:
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Flight data recorder data revealed that, after takeoff from Miami International Airport (MIA), Miami, Florida, the airplane climbed for about 16 minutes and was passing through an altitude of approximately 32,000 feet when the rapid decompression occurred. The flight crew declared an emergency (the first officer was the pilot flying) and returned to MIA. Post accident examination of the airplane revealed fatigue cracking of the upper fuselage skin above the forward left passenger (L1) door. The fatigue cracking penetrated the fuselage skin, leading to a rupture and an approximate 18-inch-by-7-inch hole that depressurized the airplane.

NTSB examinations of a section of the fuselage crown skin (from body station 374 to body station 439) where the rupture occurred revealed fatigue cracking along the lower longitudinal step of the chemically milled pocket just above the stringer S-4L (left) lap joint. The fatigue cracking initiated on the interior surface of the skin at multiple locations and propagated through the skin thickness. The skin thickness at the base of the chemically milled step measured 0.035 to 0.037 inch—which is less than the 0.039-inch minimum thickness specified by Boeing. Calculations from an NTSB study of the fatigue striation density and propagation in the fatigue region indicate that it would take an average of 3,709 total cycles for a crack to grow through skin with 0.035-inch thickness and an average interval of 917 cycles for a crack to grow from a minimally detectable size and penetrate a 0.035-inch skin thickness.

The area of cracking and rupture on the accident airplane was not subject to any specific inspections, service bulletins (SB), or airworthiness directives (AD) at the time of the accident. Following the accident, on November 22, 2010, Boeing issued SB 757-53-0097, which called for repetitive external inspections (every 30, 200 cycles, or 300 hours depending on the inspection method) to detect cracks in the fuselage skin along the chemically milled step at stringers S-4L (left) and S 4R (right) between body station 297 and body station 439. On January 10, 2011, the Federal Aviation Administration issued AD 2011-01-15 (effective January 25, 2011) mandating the inspections recommended in SB 757-53-0097.

During its investigation, the NTSB learned of a United Airlines 757 and a second American Airlines 757 that exhibited cracking in the fuselage skin similar to the accident airplane; both had nonconforming thickness at the base of the chemically milled step at the stringer location specified in the SB. Records of manufacture for the skin panels on the accident airplane and the other airplanes with fuselage skin cracking were not retained, and were not required to be retained; therefore, a cause for the manufacturing nonconformance could not be identified.
Probable Cause: Fatigue failure of the fuselage crown skin due to incorrect manufacturing of the crown skin panel that resulted in a skin thickness less than the manufacturer-specified thickness.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DCA11FA004
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
02-Nov-2010 07:53 mhab Added
10-Apr-2014 06:31 Katonk2014 Updated [Time, Aircraft type, Cn, Operator, Total occupants, Location, Departure airport, Destination airport, Source, Damage, Narrative]
10-Apr-2014 06:32 harro Updated [Aircraft type, Source, Narrative]
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
26-Nov-2017 18:35 ASN Update Bot Updated [Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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