Accident Beechcraft 60 Duke N105PP,
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ASN Wikibase Occurrence # 94
 
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Date:Tuesday 4 December 2007
Time:07:22
Type:Silhouette image of generic BE60 model; specific model in this crash may look slightly different    
Beechcraft 60 Duke
Owner/operator:Private
Registration: N105PP
MSN: P-105
Engine model:LYCOMING TIO-541 SER
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:New Castle Airport (ILG), New Castle, DE -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:New Castle, DE (ILG)
Destination airport:Allentown, PA (ABE)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to a witness, prior to arriving in the run-up area the pilot lowered the airplane's flaps. After the right flap fully extended, the flap key on the drive shaft inside the 90-degree drive assembly adapter fractured, in overload, in the direction of flap extension. Before takeoff, the pilot raised the flaps; however, with the fractured key, the right flap would have remained fully extended. The pilot could have identified this condition prior to takeoff, either visually or by means of the flap indicator, which received its input from the right flap actuator. The pilot subsequently took off, and the airplane turned left, but it is unknown at what point the pilot would have noted a control problem. The pilot climbed the airplane to 250 to 300 feet and allowed the airspeed to bleed off to where the airplane stalled and subsequently spun into the ground. Airplane manufacturer calculations revealed that the pilot should have been able to maintain control of the airplane at airspeeds over 70 knots. According to the pilot's operating handbook, the best two-engine angle of climb airspeed was 99 knots and the best two-engine rate of climb airspeed was 120 knots.
Probable Cause: The pilot's failure to maintain adequate airspeed during a split flap takeoff, which resulted in an aerodynamic stall. Contributing to the accident were the failure of the right flap drive mechanism and the pilot's failure to verify that both flaps were retracted prior to takeoff.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC08FA051
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20071227X02000&key=1

Location

Revision history:

Date/timeContributorUpdates
20-Jan-2008 12:54 JINX Added
21-Dec-2016 19:12 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:13 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:14 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:16 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:20 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
04-Dec-2017 19:02 ASN Update Bot Updated [Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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