| Date: | Friday 16 October 1987 |
| Time: | 04:00 LT |
| Type: | Boeing A75N1 |
| Owner/operator: | Private |
| Registration: | N53488 |
| MSN: | 75-2284 |
| Year of manufacture: | 1942 |
| Total airframe hrs: | 10 hours |
| Engine model: | P&W R-985 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Milton, DE -
United States of America
|
| Phase: | Landing |
| Nature: | Training |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE CHECK PILOT STATED THAT THE PILOT'S SECOND LANDING IN THE ACCIDENT AIRCRAFT WAS A 'WHEEL' LANDING. HE REPORTED THAT THE PILOT TOUCHED DOWN ON THE TOP OF A CREST IN THE AIRSTRIP WITH THE TAIL HIGH. THE AIRCRAFT CONTINUED DOWN THE SLIGHT SLOPE WITH A QUARTERING TAILWIND. ACCORDING TO THE CHECK PILOT, THE PILOT APPLIED THE BRAKES AND THE AIRCRAFT NOSED OVER, COMING TO REST INVERTED ON THE GRASS STRIP.
Probable Cause: THE PILOT'S IMPROPER BRAKE APPLICATION DURING A 'WHEEL' LANDING, WHICH RESULTED IN THE AIRCRAFT NOSING OVER. THE SLIGHT DOWNSLOPE OF THE AIRSTRIP, A QUARTERING TAILWIND, INADEQUATE SUPERVISION ON THE PART OF THE CHECK PILOT, AND THE PILOT'S LACK OF FAMILIARITY WITH THE ACCIDENT AIRCRAFT ALL CONTRIBUTED TO THE ACCIDENT.
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | BFO88DHD02 |
| Status: | Investigation completed |
| Duration: | 5 years |
| Download report: | Final report
|
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Sources:
NTSB BFO88DHD02
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
| Date/time | Contributor | Updates |
| 26-Mar-2024 12:47 |
ASN Update Bot |
Added |
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