| Date: | Sunday 27 June 1982 |
| Time: | 16:13 LT |
| Type: | Boeing E75 |
| Owner/operator: | Private |
| Registration: | N5180N |
| MSN: | 75-5439 |
| Total airframe hrs: | 2807 hours |
| Engine model: | P & W R-985 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Bloomington, IL -
United States of America
|
| Phase: | Landing |
| Nature: | Private |
| Departure airport: | Bloomington, IL (KBMI) |
| Destination airport: | Bloomington, IL (KBMI) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT STATED THAT ALMOST IMMEDIATELY AFTER TOUCHDOWN THE AIRCRAFT BEGAN TRACKING TO THE LEFT. DURING THE ATTEMPT TO ARREST THE SWERVE, THE AIRCRAFT GROUND LOOPED 180 DEGREES TO THE RIGHT. THE TAIL STRUCK TWO TAXI LIGHTS AS IT ROTATED AND THE AIRCRAFT CAME TO REST ON THE LEFT SIDE OF THE RUNWAY. DURING PRIOR FLIGHTS, THE PILOT STATED THAT THE AIRCRAFT TRACKED SLIGHTLY TO THE LEFT ON LANDINGS AND THAT HE BARELY STOPPED A GROUND LOOP TO THE LEFT WITH HARD RUDDER, POWER, AND BRAKES. FOLLOWING THE ACCIDENT THE TAILWHEEL WAS FOUND TO ANGLE APPROXIMATELY 10 DEGREES TO THE LEFT WHEN THE RUDDER PEDALS WERE CENTERED. TAIL WHEEL CABLE TENSION WAS FOUND TO BE BELOW MINIMUM PRESSURE.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | CHI82DA225 |
| Status: | Investigation completed |
| Duration: | 1 year |
| Download report: | Final report
|
|
Sources:
NTSB CHI82DA225
Location
Revision history:
| Date/time | Contributor | Updates |
| 03-Apr-2024 07:05 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation